I’m running the Storm32 V1.3 board flashed with NT217e and an Atom 3CCD Imu.
The gimbal seems to work fine except for the fact that it doesn’t start in a consistant forward yaw position.
It seems that this is caused by the failure in the last stage of the configuration to set the yaw position and then save eeprom to the board.
I get a fail every time. Very odd.
I will try powering the board with a full 12v to see whether it makes a difference.
Video to follow.